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Jesse46

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Posts posted by Jesse46

  1. Update: while up late wondering why I ever decided to get into cars, I thought about how I could simulate the motor turning over without actually turning it over, so I came up with the elaborate contraption below

    79D53459-3CC7-4AB1-888D-34DE28F10B00.thumb.jpeg.3409416b7be82da489ed23480a1fc2e1.jpeg

    I then did a triggerscope while it was turning, and got a near perfect waveform, 0 trigger errors and steady engine rpm. I think this narrows it down to bad mechanical fitment, which I’ll dig into tomorrow.

     

    0F899D61-9B86-4625-9C53-CB0475AD83B1.thumb.jpeg.ddb5362ffcee959072a0e583db37981a.jpeg

  2. During the early stages of putting the motor together, the sensor was actually rubbing on the wheel as I was turning it over by hand. I’ll attach a photo of what the damage looks like. 

    Havent checked air gap properly but I would estimate about 0.5mm. 
    No continuity from ring around bolt hole to either sensor wire.

     

    01330654-C956-4913-B2DD-EBB9621DF70A.jpeg

    2ABBB38D-E7C2-45A0-82AB-57E21A5C1F74.jpeg

  3. Hi Adam,

    Have used the loom provided with the ecu. Using the black and white cores from the black cable for trigger 1, into the black and white on the cam trigger side. I’ll attach a photo of that. Unsure if polarity is correct, I’ve tried both ways but feel the issue isn’t related to polarity on its own. And yes, the cable provided with the yelsha trigger isn’t shielded - I’ve temporarily moved it well away from any other cables just while testing.

    Cheers

    FE9AC412-F9D3-40FE-A3B8-6B49D9AB9F94.jpeg

  4. Hi there, complete noob here.


    Finished wiring my link into my rb26 and having trouble with my Yelsha D 24-1 cam trigger. Wired into trig 1 using provided shielded black & white. Set up in software with (i think) the appropriate settings. Upon turning the motor over I'm getting some super weird readings. RPM is all over the place, ranging from 140 to 3000.  Trigger errors everywhere, about 2-3 per second. Trigger scope looks super crap, unsure if its actually reading teeth or noise. Tried changing arming threshold values, rpm filtering, still similar results. Been battling with this for the last couple days and it's now beyond me. If it matters, I've been using another vehicle with jumper leads between to help crank it over. 

    I've attached a few trigger scopes with different arming thresholds, along with the base map. 

    Any help appreciated, keep in mind I'm very new to this.

     

    Cheers

    Trigger Scope Log 2022-06-27 1;32;41 pm 0.5 arm.llg Trigger Scope Log 2022-06-27 1;34;29 pm 0.2 arm.llg Trigger Scope Log 2022-06-27 1;34;59 pm 1 arm.llg rb26 current.pclr

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