VtrSp1
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Last week i have do a few track test with the E-throttle setup, downshift blip and the Ewp! All work good but i have an issue with the E-throttle, a few time when the engine is at 8000 rpm , the Throttle close a few % so the TP error accumulator go high. In another time the Throttle closed a very high amount and the Upshift isn't good The setup is with a Honda K20Z4 E-throttle Take a look at log fram 2:00 @Adamw
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@Adamw thanks a lot for help me and waste your time for that... The oscillation in the frame 3:29 it's possible to control with more tuning on the Integral gain? From my experience, the Integral gain in PID setup help to control the oscillation , or i can reduce the Proportional ? And a question about the downshift blip in the sequential gearbox with gear lever load knob cell , this based with your experience, is better dab the clutch or i can do the downshift clutchless? I have read different thinks about this, many tuners do that and many gearbox brand don't allow that with a gear lever but only with paddle shift
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@Adamw Ok so i can be happy with my setup. I have another issue that bores me, i do a test with engine off and set 100% throttle target at 0% pedal for see if the throttle blade is flat horizontally. I found that is at 95% of throttle Body and it's ok. When in the throttle target table i set the idle value (3.5 %) the blade close, go below the target and next go high. So i say that in the normal use/race use is very impossible because the foot isn't fast as a number...but i'm happy if you can take a look at log attached at frame 3.13.400 Log 2020-04-30 7;51;04 pm.llg
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@Adamw, ok i have try with the wheels up off the ground and the downshift blip work! I have a little high error accumulator on E-throttle when i do the blip or i press very fast the throttle pedal.. I have work to the PID... The P from 8 to 6 and D from 60 to 50 don't show me any improvement, but i see with a little high I from 0.030 to 0.1 the error is very low i attach the log with the last throttle PID setting that show me a low number of error during the Blip .. this is a acceptable errore range? In the log i do 3 downshift..
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I have attached the calibration used for the log i have another log The car is at 0 speed, clutch pressed and in 2nd gear. I use the lever for downshift for see if the blip work @Adamw @Adamw in The log Test 2 at frame 2.18 can you see the issue, blip throttle, ISC CL go down to -3% and engine stall..
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@Adamw , my throttle body position (Tp Main) at idle is 3.8-4% and idle stable at 1300 rpm that is the target with 80°C coolant temp. I attach a log.. i need to go from e-throttle closed loop idle to open loop because i have a ISC CL trim strange when i do the blip...it work as trim very negative and the engine shut off because the throttle go to 0% @Adamw , i attach the calibration so you can see my setting need to be testing tomorrow
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In this time of Lockdown, i have go forward with a new improve to my race car. I done this, installing a E-throttle for do a downshift due to sequential gearbox with barrell position and loadcell knob. In the past year i have the Upshift gearbox cut and all work good after few initial trouble with setting and fine tuning. The E-throttle work very good and i setup very well, i need some fine tuning on E-throttle setting but is quite easy. In normal operation it's ok, but with a Blip to 20% i have a few count on Tp target error accumulator, i think it's the PID setting . I have used a Honda K20 E-throttle and the PID setting provided in G4+ Help manual but i think the P is too high , so i try to reduce them to 7 and do a new test. The other question is about the sequential gearbox control for the Downshift Blip. - I read in other post that for a true Overrun downshift blip , the better is to shut off the Overrun fuel cut in decelleration ..this is right? This because there isn't too much time to re-activate the fuel and do the blip..? - In the Gearbox control setting , the TP LOW LOCKOUT , need to be set to 0 for allow the Downshift blip ? Normally the Overrun downshift blip start with the Throttle to 0, so if i set the TP LOW LOCKOUT at value > than 0, the ecu allow only Upshift? Or this is a bug not fixed about this setting? - The DRIVE/OVERRUN TP, need also set to 0? I have do a few test with no load to the wheels and the downshift blip work only if i set this value to 0...The test was do in 2nd gear and downshift to 1st...if i set the DRIVE /OVERRUN TP at value > than 0, the throttle blip don't work.
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I take a look at the runtime, the log memory isn't full but the internal log stop
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I have an issue with the internal logging....Often after the track session (15 min) , i try to download internal logging file and i see they are stopped automatically.. This is very a bad issue because in the most of track session i don't have the ecu log to check after the race. The log stop automatically and random before the internal memory is full I attach a log file downloaded after 14 minutes of track race..the log record only the start 4-5 minutes and after stop I have used as start condition for the log, a 1800 rpm engine speed
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Adamw, i have another question.. For double check in my log, i'm on planing to buy a new barrel position sensor with twin channel output.. Now i have the one channell version and it's configured as Gear position sensor..How i can configure the 2nd channel ?
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Adamw, Bad news for an setting update...:-( It's not possible to do it with a Virtuax Aux?For example activate a rev limiter with cut when the gear lever force is over 60 Nm or volt and start a timer for the rev limiter cut as 60 mS? My sensor not detecting the gear properly because i used a low volt tollerance 0.06V and the sensor signal often have a +/- 0.03 fluctation only in 3rd gear(Exampòe..the 3rd gear was set to 2.14 and often after the upshift o downshift i see 2.24 Volt that is out of volt tollerance), 4th looks perfect at +/-0.01 . This happens after a Box rebuild, before the signal was stable and perfect with 0.01 volt fluctation. I have check the +5V out to the sensor, the ground but all looks good. The magnet on my barrel is clean with no debris . I have try to rotate the sensor on the box cover to 20°, i re-done the gear position setting and now after a few upshift and downhisft with no load to the wheels, the signal are more stable.. I attach a log and the calibration , the log show the few upshift and downshift in sequence new gear setting.llg new mods- boost control - gear setting.pclr
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This is what happen..
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Adamw, I have an opposite situation.. the sensor report a signal Little low that is out of the volt tolerance so the ecu show me 0 gear but in real I’m on 3rd.. I pull the lever for upshift and the ecu start the cut from 0 but after 8 mS see 3rd gear and end the cut in 8mS.. so if I have a minimum shift time at 70 mS the power is not reintroducing early
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Adamw, it's possible to set a minimun cut time when the cut end is set to barrel position? This can help in a endurance race to minimise damage to the box if the gear position sensor or other fail.. So example..if i have the low upshift time at 85 mS, i want to set a value for minimun cut time to 70 mS
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I have a Honda S2000 F20C My 2000 customer car that need a race ecu and i'm interested to use the Link G4+ Extreme and do a full engine wiring harness. The car have the stock Dashboard so the coolant gauge work with a multiplexer (can honda line) direct to the Ecu stock. My question is about the stock coolant gauge, it's possible to have it fully working with the LinkG4+? I have used a few times for the Honda S2000 an AEM Infinity ecu and all work good, the coolant gauge also and in the Infinity Instruction , Aem tell how the stock coolant gauge work... I attach a screenshot , hope anyone can help me :-) this is the table setting about the LS6 in the Aem Infinity calibration
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Mapper, i have check my log and the cut stay On when the gear detected is 0
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Mapper, i have try with 20% fuel enrichment in one track lap and i can't prevent or soft the big bang in the exhaust. I'm about interested to your value about the fuel cut 60-85% and 40 deg retard... In my experience, low gear need more fuel cut % than the high gear. The 40 deg retard is interesting, with only 15 degree retard i have a power reintroducing too soft and the engine bog... In my car, at full boost the ignition is 15-16 ° Btdc, so if i retard more than 10 °and more than 20 mS time , the power re-introducing is too slow and i feel a loss of power in the upshift. The gear 0 detected between the shift is strange . I think the ecu use the strategy looked at the start of upshift and they don't change if during the upshift the value gear go to 0
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Adamw, after some track test with the race car i have interesting data about the shift cut strategy.. All test was made in the same track with same car setting (tyre, power level etc) - Ignition cut at 90% , ignition retard -10° and no Extra fuel trim in the shift cut strategy. Pros: cut instant, fast and hard, no fuel lean after the cut end strategy , no gear re-bounce Cons: Hard bang in the exhaust that can destroy the turbo /manifold and also engine - Ignition cut at 90% ignition retard - 10° and add a fuel trim +10% in the cut strategy Pros: cut instant , fast and hard , no gear re-bounce Cons : Hard bang in the exhaust and the 10% extra fuel trim don't solve the exhaust bang. The exhaust bang is same as without the +10% fuel trim - Fuel cut at 90%, ignition retard -10° and No extra fuel trim in the shift cut strategy Pros : shi ft lever feel smooth , no exhaust bang Cons : cut not instant and fast as the ignition cut ( i use a low Gear lever force Nm for start the cut before), and if the shift Lever travel isn't full and very precise i have a 2 time a gear re-bounce (shift from 3 to 4 and the box return in the 3 th gear). A lean situation after the gear cut strategy end - Fuel cut at 80% , ignition retard -10° and no extra fuel trim in the shift cut strategy Pros: shift lever feel smooth than fuel cut 90% , no exhaust bang Cons: cut not instant and fast as the ignition cut, 1 times a gear rebounce and lean situation after the cut strategy. So for the cut power is better the ignition cut (it's fast and instant and i haven't gear re-bounce) but the downside is the bang in the exhaust. Do you think with a low % of ignition cut, the exhaust bang is reduced? The other test is reduce the ignition cut % to the number that can't give me a dog disengage for see what is the low % allowed for the dog disengage and after try to use a little high % than the minimun finded but not too much? If i use a 10% fuel trim in the shift cut strategy, this can help me in the lean situation after the fuel cut strategy for upshift?
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Adamw, this is some picture about the wiring from the customer car
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i have a Mitusibishi Lancer Evo9 with the PlugIn ecu and a Aim MXS Strada Dash installed, but i can't see any data to the Aim Dashboard. The Aim Can wire is connect to Can1, i have check Can High- Can Low wiring and it's ok. My Aim Ecu Stream is set to LINK-CAN_BUS_BASE_LCC and the setting on the Link Ecu CAN Setup is in the picture attached . I take a look at the runtime value for the CAN1 and i see a error, in the picture attached can you see the Runtime Error for the Can1. I have switch the can connector to CAN2 , setting them proper and the error appear in the Can2 Can you help me?
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Adamw, don't worry for the slow reply :-) My "start shift validation time" is set at 2 ms. My upshift gear lever force is set to 44 Nm , i check a few log and the cut start before the barrel move (i take a look at gear lever force and barrell mV value). I can try to low the upshift gear lever force a bit but i think i can have false trigger when in the track.
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Adamw, thanks a lot for the awesome explain !! Your explain is about same as my when i see the log after the race . The cut time in high gear (3-4-5) is about 70-80 mS and it's not bat for me, it's the time that i expect from this type of gearbox with shift lever. I think it's possible to improve- reduce this time with modify the mechanical rotational mass (more light flywheel and racing clutch without with small diameter unsprung). The logs show the power is re-introduced with the barrel is still moving, normally this can cause premature dog wear... What i can do for have the re-introduced power with barrell stopped? I can play with a lower gear tollerance? The lever fell smoother but not smoother than if i dab the clutch for the same shifting.. In the first part of lever pull i feel a hard shot ("tac ") with the Upshift and this isn't present when i dab the clutch or left the foot from the throttle to unload the dog... I have the same issue a few month ago when i used for the Gear cut the Geartronics EasyShift Ecu (coil cut) in closed loop mode. This strange feel in the lever i think in the log is showed by the firs peak of loadcell signal..
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Adamw, thanks a lot for the helpfull reply . Very interesting the strategy for quite the exhaust bang with add fuel in the shift...normally i see the opposite, so cut the fuel at 100% for don't have extra fuel washing the exhaust with ignition retarded. I want to remove all bang possible due to better life of turbo and exhaust manifold. I take a look at my gear lever force and i see the dip of force but if you can see and give me some consideration about that , this is very helpfull for me :-) I have a internal log at 100 Hz of my track session , so i can upload and you can take a look at my gearshift parameters. I logged at 100 hz all the shift parameters.
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I have a G4+ Fury installed in my race car with sequential gearbox. The ecu is awesome and all work very good. I need only a few clarification about the Sequential Shift Parameters/setting . As i mentioned before, i use the ecu to do the Shift cut for my Sequential Gearbox in Closed loop mode with Loadcell Knob and Gearposition sensor with Ignition cut % set at 90% and a Ignition Reatard at -15° for reintroducing torque strategy at 20 mS. In the Last weekend i tested them on track and when i do the Upshift strategy i have a big bang in the exhaust . it's normal because i cut the ignition at 90% and the rest 10% is retarded at -15°. I set the retard to -15° because i feel the shift lever smooth than a -10° retard. I have try to set the Fuel trim shift cut to a negative value to reduce the fuel amount in the shift cut but it's not possible to insert a negative value. How i can remove fuel in the shiftcut strategy to reduce the bang in the exhaust? In the log i take a look at Gear Parameters and when the barrell move, the Gear number go to 0 for a little moment during shifting. My Gear tollerance is set to 0.1V because i want the shift cut quite safe. If the Gear tollerance is low value, the power re-engage is safe for a full dog engage vs a high gear tollerance number?